So it’s been almost a month since I’ve posted anything. There’s a great reason for that. I’ve been spending crazy amounts of time getting a new kitchen cabinet set complete prior to my kitchen renovation. After all, why buy inferior cabinets or over priced high quality ones when you can make them yourself right?
That said so far I’ve ended up with nearly 200 raw videos of making this entire set, which to meet the deadlines I have, leaves very little time for editing all those videos into my Kitchen Cabinet Series.
Once I get everything complete I should have more time to edit the videos and get some video content posted.
In the meantime however here are some progress pictures.
First there was one cabinet, then two, then three … you get the picture.
Do you have a dresser drawer that has a bottom that has sagged down? I had this happen to me with both my daughter and son’s dressers. As it turns out the fix for both of them is really simple, it just required a little time for some glue up.
So, first things first – you need to unload the contents of the dresser drawer and pull the drawer out. In my case to remove the drawer was as easy as fully extending it and giving it a slight lift up at the drawer front while pulling out. This allowed the slides to separate and the drawer to be removed.
Once I had the drawer removed I just had to separate the back of the drawer box from the rest. This allowed the drawer bottom to slide out. My solution was to put a small strip of wood underneath the front of the drawer bottom panel. In order to glue it up I needed to remove any finish and stain that was on the backside of the drawer front. If you skip this part chances are the glue to hold the strip of wood on will not adhere. I used Titebond Wood Glue to glue the small strip I cut, clamping to keep some pressure on it.
Once the strip was glued in, I added glue to the groove the drawer bottom slid into and slid the drawer bottom back in. I then screwed the drawer box back panel back on. I continued by wiping up any glue squeeze out and let the glue set up over night.
Then it was just putting the drawer back in the dresser and putting the contents back in.
In this video I show what I did to fix the drawer. I hope you find this video helpful.
First let me say it has been a while since I have made an update. This is partly in fact because I have several on-going projects that I am working on along with busy spring / summer activities. Several are complete but I have not had time to edit the raw videos into a nice presentation and the others are ongoing still.
So – what is done but not edited yet?
I painted the walls and refinished the floors in our spare bedroom. This is where we planned on moving our daughter into from her smaller child room. Here is just one of the pictures of the floor. After she was moved into this room I got a chance to do the same (paint and refinish) to her old room.
My son’s dresser drawer bottoms were falling out on 2 of his drawers so I need to fix them. Who hasn’t purchased clothes furniture that has 1/8″ thick drawer bottoms and not had issues like this?
I built a longer sacrificial fence for my table saw. This will be used for a project that I’m currently working on – Complete Kitchen Cabinet Replacement. You can even notice some of the rough Maple lumber to the upper left for that project.
So what is in progress?
Here are 5 of the 14 face frames I need to make for our new kitchen cabinets. The frames will be maple painted white with Maple veneered plywood for the cabinet boxes with a clear finish – at least that’s the plan.
My vertical blinds started getting some slats that were no longer turning. My first thought was to replace the entire blinds so they matched the others in the house but after getting a price estimate I decided that was no longer an option. After all, fixing something many times is much more cost effective than replacing something outright. So I decided I would try to repair them instead
In this video I’m repair my Graber Vertical Blinds which have been in my house since I purchased it many years ago. I don’t remember exactly when but one of the center slats was not turning anymore. I pretty much just wrote it off as okay, I will ignore it or eventually getting around to fixing it.
As time progressed this one slat plus the how close my couch was to them started causing others near not to turn. Still rather than correct the problems we decided to ignore them and only correct the effects rather than the symptoms. Well as more time progressed the blinds became increasingly annoying to open or close because the slats were interfering with each other. Now was the time to address the issue.
Initially as I stated we thought about updating them to match the other blinds in our house – only to be shell shocked by the price estimate. We knew what the other ones cost but the estimate came in for this one – nearly $800 for just this one and not the same brand but a less expensive one. Yeah – no thanks and the decision became can I repair them. I fixed the stems but didn’t realize there was a missing scissor track gear when I ordered my parts.
This video illustrates how I went about replacing the failed components which took less than 60 minutes to complete.
So I own a Moen Extensa Kitchen Faucet. This particular model has been discontinued but is still a great working faucet that has Moen’s Lifetime Warranty. So whenever anything goes wrong I take a picture or two, write up a short summary of the issues on Moen’s warranty claim and wait for the parts.
In this video I’m repairing the faucet with a new Dome, Handle and Handle Adapter Assembly. My faucet is the Chrome model but others will have nearly the same kits except for the Dome (and any other parts that are on the surface). This faucet has a heavy handle which appears to cause issues over time – nearly 1lb. This time the dome managed to pop up and got damaged to the point where in order to shut the faucet off we had to push down at the point where the faucet connects to the handle hardware and cartridge.
This video illustrates how I went about replacing the failed components which only took about 30 minutes to complete.
So it has been a while since I posted anything. Rest assured nothing is wrong with me, I have just been busy over the holidays by which I mean Halloween, Thanksgiving, Christmas and New Years.
Anyone how knows me knows that during this time I am obsessively cleaning my yard of fall foliage and prepping it for winter and well, Christmas lights.
My interest in Christmas lighting has been with me since I was a little child and well has only grown over the years. Now, it has blossomed into a large display – one that is peaceful and serene – not something flashy. This year, I had other elements to incorporate into my design as we are currently undergoing two bathroom rehabs so I could not resist decorating some temporary yard residents. After all, how else someone decorate a dumpster and a porta-potty. You can notice these elements begin to take affect through the different pictures below.
Below are some of the pictures I took of this years display. I try to not do the same thing multiple years and generally try to get more creative each year. I usually end up spending between 20-36 man hours which includes getting the lights out, stringing them and putting them away when over.
My electric Whirlpool dryer stopped drying because the heating element stopped working. I decided to take it apart and see if it was worth fixing or not. After all, fixing something many times is much more cost effective than replacing something outright. Please note that fixing a high voltage, high temperature appliance such as an electric dryer should only be done if you are comfortable doing so as incorrect repairs may result in electric shock or fires.
Once I opened the unit up I found the Hi-Limit thermostat had essential destroyed itself. Generally this will happen if it is not working properly AND one of the lower temperature setting thermostats also fails.
Fixing it was not really that time consuming or difficult. Once I had it open I was able to match the OEM part numbers with replacement parts. One of the parts had be discontinued so I had to use an adjustable thermostat. I just needed to set it to the correct operating temperature as denoted by the instruction table that it came with for the adjustable thermostat.
Once the parts arrived I removed the Hi-Limit thermostat with fell apart when I removing it. I had to put in a pig-tail wire (10AWG) matching the original wiring. This was required because the original had over heated and burned the wire. The the Hi-Limit thermostat replaced I turned my attention to the other thermostats. I needed to figure out which was bad. At cool temperature a continuity check of all three of them showed they were good. So, one (or more) had to fail at the shutoff point. You can check this by putting them on a skillet or griddle and raising the temperature to the point where they are supposed to trip. In the case of mine, there’s a about a 5 to 10 degree difference between each one.
However, since I did not really feel like taking them all out I decided to run the dryer and start at the low setting. If it turned off prior to the Hi-Limit, it was good. I proceeded through all of them and one failed. I replaced this one with the adjustable thermostat setting the temperature to setting D which for my part was 150F. I hooked everything back up and did one final temperature check cycling through each setting. Everything was working perfectly again.
Finally since I had the back of the dryer open I decided to clean up the lint. This is always a good idea to do once in a while to prevent lint build up which can be a fire hazard. About 3/4 the way through vacuuming I realize my Shopvac was not fully snapped down so small dust, dirt and drywall particles start flying around the room. I guess I had to clean that mess up now as well!
The replacement parts I used were from www.appliancepartspros.com. They provided easy ordering and quick shipping. My adjustable thermostat did not come with the instruction table so I contact them via chat and they were able to email me a PDF of the instructions. This was great service.
Have you ever went to turn on a lamp – one with a turn knob – and it just does not turn on but the knob turns without clicking? Well, that is what has happened to me. There is no need to throw away that lamp and buy a new one. I paid about $5 for a new turn knob socket at one of the big box stores. It does not take much time at all to replace and is quite satisfying when that light turns back on.
So, if you have a problem like this, hopefully you will find this video handy and it can save you some money.
In this video I show what I did to change out the failed turn knob socket from start to finish. The process is quite simple. Please give a thumbs up and do not forget to subscribe.
So my family and I went to see Monster Jam in St. Louis in 2018. We went to the Saturday showing. This year we did something different. We purchased the Pit Party Passes so we could go down on the field prior to the show and see the trucks and drivers up close in person.
It was pretty cool seeing the trucks up close like that but our friends that have done that before were correct, the lines get long if you want autographs and they “close” the lines roughly 30 minutes before the drivers have to go away for the show. Our friends recommended the divide and conquer method in which one parent goes to one line, the other goes to the other and the children go to whichever parent gets to the driver first, alternating this system back and forth.
After the Pit Party closed down went and got some food to eat at our seats. The food was C- at best – cold, skimpy on the portions and overpriced.
Prior to the show starting we dawned our Ear Muff protection – previous years our youngest had ear muffs and the rest of us used ear plugs. This year both kids and myself had ear muffs and only my wife used ear plugs. Much better hearing protection in my opinion.
So the show starts and we discovered what is becoming and definitely became as you can see from the following videos is that we had numerous families around us that couldn’t stay seated. They were in and out multiple times. In fact the family of 6 right next to us was in and out at least 8 times. Not all at once, generally 3 at a time which made it more annoying.
The show was a little more boring this year than previous years and the 2 wheel competition reminded me of a shortened freestyle competition except focusing on keeping the trucks on 2 wheels.
The show went on following the usual format – Intro, Heat Races, 2 Wheel Competition ending with the Freestyle Competition.
Here is some videos I put together of each segment and the entire show. I hope you enjoy them and if you do, please subscribe to my channel and give the videos a Thumbs Up!.
I went to use my Harbor Freight hand truck and one of the tires was flat. I aired it up and went to use it but it quickly went flat again. Turns out I had a hole in the inner tube and it needed replacing. I purchased a replacement inner tube (4.10/3.50) for the wheel at Harbor Freight.
So, if you have a problem like this, hopefully you will find this video handy and it can save you some money.
In this video I show what I did to change that inner from start to finish. The process is quite simple. Please give a thumbs up and do not forget to subscribe.